FordPro
New LVC Member
I'll try the leakdown method for sure. My compression gauge goes in hand tight and the adapter I put into place to fix the plug hole doesn't allow it to thread in enough for a proper comp. test. Reads way low even for a bent/sucked valve or even shattered piston. Yeah the piston is banged up good from the plug and what ever else. I'm gonna pull the head to inspect, man I need a daily not this bs. Fords shoot plugs because of bad design period, almost no other heads spew plugs like this. Thanx ford engineer scum bags! Yeah it was a big metal noise, not some aluminum shavings. Thanks bro keep me informed.